Saturday 23 January 2010

Time to Re-Wire the Brewery

I brewed last night and things didn't go according to plan!

The temperature controller that I use to maintain the temperature of the wort as it is recirculated through the heat exchanger just wasn't showing a stable temperature.  It fluctuated by as much as 20°C so any kind of control was out of the question.  I have had this problem before and I know it's down to moisture in the wiring which I've been putting off replacing for months.  I think I now have to bite the bullet.

I managed to get through by monitoring the temperature of the mash tun and the heat exchanger with a thermometer and controlling the heat exchanger manually.  A few pints of AK helped me along too!


In case you want to see the recipe here it is:

Chineham Pale Ale
Brew Length (L):          55.00
Total Grain (kg):         9.40
OG:          1.040
Anticipated EBC:          29.6
Anticipated IBU:          31.0
Brewhouse Efficiency:       75 %
Wort Boil Time:             80    Minutes


Grain/Extract/Sugar

   %     Amount     Name                           EBC
-----------------------------------------------------
 87.8    8.25 kg.  Pale Malt(2-row)            7
  5.3     0.50 kg.  Crystal 55L                     145
  5.3     0.50 kg.  Flaked Corn (Maize)      0
  1.6     0.15 kg.  Black Patent Malt            1390

Hops

   Amount     Name                              Form    Alpha  IBU  Boil Time
-----------------------------------------------------------------------------
 55.00 g.     Fuggle                              Whole    4.40  12.6  First WH
 55.00 g.     Goldings - E.K.               Whole    4.20  12.1  First WH
 40.00 g.     Fuggle                              Whole    4.40   3.2   20 min.
 40.00 g.     Goldings - E.K.               Whole    4.20   3.1   20 min.


Yeast
-----

White Labs WLP002 English Ale

3 comments:

  1. What a pain. I brewed today and had a few issues too. It must be the time of year.

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  2. Yes I've just seen your post. The cold and damp are a pain. You were lucky to fix that chiller before it ruined all your wort. I'd never have thought it would have got cold enough in your garage to freeze your chiller.

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  3. The chiller was in the shed. I was amazed how much the copper had expanded. Thank God it was only two splits. One was quite long but I managed to approximate the edges very well. I learnt how to repair holes in copper cylinders etc will solder from my father-in-law. You have to be patient and know when to say "that's good enough" rather than being a perfectionist.

    I am planning to install the brewery in the garage (a bit like yours) which will save be a lot of assembly time and reduce the dampness and freezing! also I found today that the shed roof is very badly in need of re-felting.

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